This has been very exhausting experimentng for a solution for my MYVI 1,3 Auto tranny Exhaust Solution.
I have purchased from a friend HotBits 4 to 1 Extractor which was fitted nicely to replace the stock extractor.
At Beginning the Extractor mod alone has brought in large difference in pickup for my Auto Myvio but still the power seem to be blocked and rpm is high before
actual power is felt and delivered..
I contacted Kweng for his recomendation according to my Budget..
I informed hin that my Issue was low to mid power restriction/loss due to the stock bullet and s-mufler.
He initially recommended that i only change the S-Mufler . I head myself to GT Racing Workshop in puchong to try to solve my issue.
After Meeting his mechanic in Puchong .. the Mech spent a lengthy time to explain his experienced on modding a Myvi 1.3Auto.
According to this Mechanic I need to change my hole front piping from the stock 1.6" to 2" and rathwer then changing the stock S-Mufler only change the Bullet.
They developed a Bullet Design to solve the "kick Back Effect " which was originally delivered by the CatCon.
This Cat Con apparently according to the mechanic not only is used to absorb harmful gas but also utilise by the car to push the low-mid range rpm that was needed
that was lost during Auto Transmission.
The Solution was to take a 12" Straight Flow Bullet and put in a slighly smaller pipe maybe 2-3" in length and fit it into the inner diameter of the Bullet. This smaller full pipe will block some of the perforated holes that exist inner side of the bullet. This somehow will create a "Kick Back" effect similar like the Cat Con.
The second stage was to replace the 1.6" stock pipe right from the joint of the Extractor to the Bullet itself. This will be end to end 2" pipe.
I was trully confident and the skill that the mechanic has. He seems to know what his doing since he mentioned he has done this method for lots of auto Myvi.
The Job was done. Now time for testing...[I]
I noticed the following..
After Changing the pipe from 1.6" to 2" the sluggish effect still exist and now the power band which exist before the mod has now decreased. Before the powerband starts from 2K up to 6K . Powerband now onlly starts actual at 3K to 6K. This somewhat produce the Screaming effect. Which is audible from the 12" bullet Mod. I really have to push the peadl to ensure that power is delivered. The power is not as effecient as before..
I have tried to contact Kweng on this issue it seems he is busy even to answer my SMS. I want to make it clear that.. if the Issue was the upgrade to 2" piping please confirm it here. As the workshop insist that the piping be changed. Since the mod i have extensively read Lowyat and Zeroto100 forum and most thread mentioned for Auto Tranny it is not adviseable to change to a bigger diameter piping. This will in turn increaseFc and makes the car feels like it is struggling to be pushed.
I am confused regarding the conflicting solution that the Mechanic and Kweng offered. I think my issue can be solved by fitting back the old 1.6" piping to the new bullet or better to change to the new 1.6" piping if the cost is not reimbursable.. but i need a solutin asap.
I know Kweng has good reputation in Lowyat interms of exhaust . I hope Kweng you can answer this issue asap.
JOe
This post has been edited by mizzdelina: May 6 2011, 06:45 AM
Performance Parts [WTS] COMPLETE CAR EXHAUST SYSTEM (CUSTOM-BUILD), Who says CHEAP NO GOOD?!
May 6 2011, 06:11 AM
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